This
Day In History
Summary
of Events for No.
439 (CAN) Squadron
as
compiled by C20089
F/L M. Harrison
in the 439 Squadron Operations Record Book Form
540
for
26
January 1945
B-78
Holland
Heavy
ground haze for the day with fairly low overcast, but two
operations were carried out in the morning. Bridge and snack
sessions and reading absorbed most of the time. In the face of
heavy snow after supper, the pilots wended their way to the
Officers Club at Aalst where we celebrated the promotion of F/L
Jim Beatty to the rank of Squadron Leader who is now officially
the Squadron Commander and F/O Lyal Shaver Flight Commander of
"B" flight. F/L Coffey has gone back to 438. About two
days ago surprising news was received that S/Ldr. Crosby is
safe. The immediate improved morale was exceedingly obvious.
The few aircraft which exploded on operations had undoubtedly
bewildered the new pilots and they were quite shaken, being
suspicious of the safety in flying the Typhoon. F/L Johnny Carr
and F/L Joe Kyle, ???,
went down to see him at 39 British General Hospital at Hesselt
where Bing was in good spirits and gave a blow by blow
commentary on the explosion of his aircraft.
On
the 22 of this month he led the Squadron on a dive bombing
operation on Uetterach and after releasing his bombs, his
aircraft was clobbered by accurate heavy and light flak causing
it to explode and disintegrate. He attempted to pull
his rip cord of his chute twice and since nothing happened he
found his right hand to be U/S (unserviceable).
At 1000 feet he pulled the cord with his left hand and sailed
earthward landing 100 yards from Uetterach and after rolling up
his parachute he found refuge in a nearby wood where he lay
wrapped in his parachute for 36 hours in intense pain
unmolested, although Jerries worked within 10 feet of him at
times.
On
the 23rd this town was again bombed by our Wing and S/L Crosby
got quite a shaking and a layer of dirt and debris. Following
his recumbent period of 36 hours and after being frosted up a
bit he decided to make for our lines only four miles away which
he reached safely on eluding enemy sentries and ran into the
British Army which assisted him to 39 British General Hospital
and was subsequently transferred to 24 ??
. CCS.
on the 24th.
The
injuries sustained by Bing were a dislocated right shoulder and
frost bites. Incidentally 1000 pounders are not to be used until
further notice pending investigation of the explosions of
aircraft on operations and for the present 500 lb. bombs, 11
second delay will be utilized. Another aircraft was transferred
to Maintenance reducing our strength to 10 and all are
serviceable. Two operations consisted of the total flying for
the day.
Detail
of Work Carried Out by
No. 439
RCAF Squadron
as
recorded by
J20602 F/O R.H. Laurence, J29881 F/O W.G.
Davis,
and
C20089 F/L M. Harrison in
the
439 Squadron Operations Record Book
Form 541
A/C
Type & Number |
Crew |
Duty |
Up |
Down |
MP151
RB499
RB377
RB198
|
F/O
Shaver L.C.
F/O
Elsley D.C.
F/O
McBride A.C.
F/O
Cleghorn D.G.
|
Armed
Recce
|
08:50 |
10:05
09:55
10:05
10:05 |
Details
of Sortie or Flight
F/O
Lyal Shaver, leading four aircraft, took off on an armed
recce into the Coesfeld area. The weather was expected
to hamper operations, but it turned out to be
serviceable. A train was sighted just south of Coesfeld
which was strafed. Another train minus locomotive was
also peppered. Some 40 M.M. was noticed on the first run
in, just south-west of Coesfeld.
The Squadron then
climbed up and set course for base. On crossing the
bombline Red 2 (F/O Don Elsley) a new member of the
Squadron called up to say that he had developed engine
trouble. His temperatures were all OK, but a loss of
power was noticeable probably due to fuel or ignition
trouble. Elsley finally had to bring his aircraft down.
He forced landed successfully at E759193, although the
aircraft was badly mauled in the radiator, port wing and
fuselage, after crashing through an iron fence and a
ditch, rendering his aircraft a Cat B.
The remaining
three aircraft returned to base, all landing safely.
Claims - 2 loco damaged, TRC - 2 damaged.
|
A/C
Type & Number |
Crew |
Duty |
Up |
Down |
RB281
RB233 RB262 PD564
|
F/O
Davis W.G.
F/O
Marlatt S.D.
F/O
Anderson W.
F/O
Roberts J.
|
Dive
Bombing
|
11:35 |
13:00 |
Details
of Sortie or Flight
Four
aircraft, finally got airborne after sitting at the end
of the runway at readiness. F/O Lyal Shaver was the
leader of Red Section, who had taken off previously, and
pronounced the weather as serviceable. F/O Bill Davis
led his section, heading for the Coesfeld area, and it
was on targets of opportunity. A stationary train was
seen south of Coesfeld near Lette and the boys took two
passes at same. There was very little flak except for a
lonely 20 M.M. type who quickly ceased firing as soon as
he knew our boys meant business.
All aircraft returned
to base, with noticeable deterioration in the weather.
Claims - Locos - 1 damaged, TRGS - 8 damaged.
|
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